After a hundred mile ride to lunch today I decided to try gearing the bike up one tooth in the front to see how it would react. The motor seemed to be "busy" (turning too many RPM) at an indicated cruising speed of 48 MPH and I thought if it would pull one more tooth in the front perhaps it would not only make it feel less busy but also improve it's cruising speed.
I'd previously put an "O" ring chain on it in the stock length but unfortunately it's too short to accept another tooth
. Off to the shop and I bought a regular #428 chain to experiment with. It took 108 links to mate a 15 tooth sprocket with the standard 36 tooth rear (stock is 106).
Wow!! It still never fails to amaze me how gearing affects how a bike runs. The bike now goes faster in each gear before shifting and will cruise at an indicated 52-55 MPH (actual 49-52 MPH according to my GPS). This is pretty much equal to the Lifan powered Passport I rode to the Smokies from Indy last summer that I was using as a standard.
I'm sure in hilly country I'll be shifting more and next weekend I'll make another run to the hills to see how it reacts.
If you don't have to have an "O" ring chain this is a cheap change with the chain around $20 and the sprocket about $7 on eBay. As mentioned this is a #428 setup and the front shaft is the same style/size as the older Hondas with a 17mm shaft (the Lifans use a 20mm output shaft).
Now I've gotta buy another "O" ring chain. At least I can run the first one on another step through project I'm building.
If you want your bike to feel less busy and have a higher and more comfortable cruising speed give this a shot. I think you'll like it.
Temperatures today got up to around 80 and the bike seemed to be running a bit rich at about 1/8-1/4 throttle opening on the Mikuni I'm running. First I stopped and removed the steel washer I'd put under the clip and up the road stopped again and removed the brass washer leaving only the nylon one. Both helped so I stopped again and swapped the brass one for the nylon one which visually is slightly thinner and again got an improvement. The next step will be to try dropping the needle one notch and then juggle the washers to see what works best.
Life is great sometimes and this was one of those exceptional days when my experiments went well.